Design and Implementation of Multi-station Palletizing System Based on PLC Control

CHEN Rui-hong

Packaging Engineering ›› 2018 ›› Issue (17) : 159-164.

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PDF(1197 KB)
Packaging Engineering ›› 2018 ›› Issue (17) : 159-164. DOI: 10.19554/j.cnki.1001-3563.2018.17.026

Design and Implementation of Multi-station Palletizing System Based on PLC Control

  • CHEN Rui-hong
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Abstract

The work aims to expand the effective working scope of industrial robots. A set of complete movable chassis system for industrial robot was established with MITSUBISHI Q series PLC and location module QD75MH1 to mobilize the location of the robot and effectively expand the working scope. Taking four-station palletizing and packaging workstation as an example, the system worked stably, and the working scope of industrial robot was expanded to 4 stations from 2 stations. The work of 4 stations could be com-pleted by 1 industrial robot and the packaging efficiency was increased by 2 times. The system has a good reference value in multi-station palletizing, packaging, handling and other occasions.

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CHEN Rui-hong. Design and Implementation of Multi-station Palletizing System Based on PLC Control[J]. Packaging Engineering. 2018(17): 159-164 https://doi.org/10.19554/j.cnki.1001-3563.2018.17.026
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